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Author Topic: 1987 Bridgeport Production Center Interact 412 to Mach3 Conversion  (Read 17589 times)
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JHChoppers
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« on: December 09, 2009, 11:10:50 AM »

We pick up this machine about a year ago, and we now starting to dig into it.   This 412 was used in Tech School for most of its life.  Then a machine shop got it next and ran it until it broke.  The tool changer failed and they we having issues with Y Axis. 

Below are pictures of loading it as we prepared for the 425 Mile trip back to my shop:


* BP_VMC1.JPG (694.75 KB, 1000x750 - viewed 527 times.)

* BP_VMC2.JPG (732.7 KB, 1000x806 - viewed 217 times.)
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JHChoppers
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« Reply #1 on: December 09, 2009, 11:26:41 AM »

The BP412 sat on the trailer for about week, as we tried to figure out an elegant why to unload the 5800lb chunk of IRON.  We ended up calling a local wrecker service, one that is large enough to pull crashed semi’s off the road.  They have fork trucks and wreckers,
and are experienced in unloading/loading crazy things from crash sites.

Here are the pictures of them unloading it from the trailer and placing it in the shop:


* IMG_4031 (2).JPG (803.15 KB, 1000x750 - viewed 335 times.)

* IMG_4033 (2).JPG (711.63 KB, 1000x750 - viewed 311 times.)

* IMG_4034 (2).JPG (780.37 KB, 1000x750 - viewed 223 times.)

* IMG_4043 (2).JPG (732.34 KB, 1000x750 - viewed 481 times.)
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Overloaded
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« Reply #2 on: December 09, 2009, 12:26:47 PM »

WOW.....looks good Joel.
Keep us posted on the progress.
That's one tough little trailer too !
How well did it tow ?
NICE,
RC
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JHChoppers
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« Reply #3 on: December 09, 2009, 12:29:36 PM »

Most of the sheet metal and the coolant pan were removed, so we could get easy access to the servos, belts, ball-screws, tool changer and wiring.  New paint and will added to the skins and some of the IRON when it’s reassembled.  


* IMG_5589 (2).JPG (782.81 KB, 1000x1065 - viewed 341 times.)

* img_0218 (2).jpg (859.04 KB, 1000x860 - viewed 462 times.)

* IMG_5614 (2).JPG (830.72 KB, 1000x965 - viewed 690 times.)
« Last Edit: December 09, 2009, 12:37:06 PM by JHChoppers » Logged
JHChoppers
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« Reply #4 on: December 09, 2009, 12:34:25 PM »

WOW.....looks good Joel.
Keep us posted on the progress.
That's one tough little trailer too !
How well did it tow ?
NICE,
RC

Yea, that trailer is only rated for 6000LBs.  It road fine, we just keep it at or under 55 mph.  Nerve racking to say the least!  LOL
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Dan13
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« Reply #5 on: December 09, 2009, 01:19:05 PM »

Wow, on that first picture where they unload it from the trailer, it can actually be seen that the structure is bending above the chains. Did you check the bed and slides were Ok?

Daniel

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JHChoppers
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« Reply #6 on: December 09, 2009, 01:50:57 PM »

Wow, on that first picture where they unload it from the trailer, it can actually be seen that the structure is bending above the chains. Did you check the bed and slides were Ok?

Daniel



Yea, it looks worse than it is.  On those old 412s, the sheet metal is in multiple parts and is supported only by the legs on the floor, its realy attched to the machine.  The real machine IRON part just sits inside the sheet metal box on the floor all by itself.  So when the machine is moved by the IRON, the sheet metal just hangs like floppy dog ears.
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JHChoppers
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« Reply #7 on: December 09, 2009, 02:35:44 PM »

The old electronics were working when we picked up the machine, since there is market to sell them, we did.  Some might think it is better to use the stock components and this is a good argument.  However, we want to be able to repair the machine ourselves in the event of an electronic failure, both quickly and at a reasonable cost.  By upgrading to newer components, we can easily interface to Mach3 and keep or energy footprint low.

The goal is the run the BP412 at 220VAC 1 Phase 40Amps

Pictures of the stock parts:


* img_0476 (2) (2).jpg (693.97 KB, 800x1066 - viewed 232 times.)

* img_0477 (2).jpg (973.03 KB, 1000x750 - viewed 217 times.)

* IMG_5663 (2).JPG (880.12 KB, 799x1066 - viewed 246 times.)

* IMG_1315 (2).JPG (650.26 KB, 1000x750 - viewed 230 times.)
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RICH
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« Reply #8 on: December 09, 2009, 04:38:29 PM »

LOL with the addition. Hopefully it will enhance the shops capability and production.
Post when she's done and looking pretty.
RICH
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JHChoppers
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« Reply #9 on: December 09, 2009, 05:10:46 PM »

With the all the old electronics removed, it is time to start building up the Basic Mach3 System.  First things first, Breakout Board and Charge Pump.  I really like the Charge Pump integrated in Mach3, this allows for ALL outs to be tri-stated when the system is not RESET.

The only part we kept in the electronics cabinet was the 3 Phase Power Switch.  We ran 220VAC to the switch fused with 40AMP breaker, so we have 110VAC or 220VAC available on the output of the switch.  A switcher PS provides 5VCD and 12VDC, an analog PS was used 24VDC, and a transformer is used to generate 90VAC and 200VAC.  The solid state relays will be used to switch the pneumatics for the tool changer, enable the oilier and the control the Spindle 200VAC Cooling Fan built into the spindle.  A second relay is connected to the charge pump out to enable the 24VDC Z Axis break.


* IMG_1318 (2).JPG (955.03 KB, 1000x1333 - viewed 145 times.)

* IMG_1317 (2).JPG (563.74 KB, 1000x750 - viewed 156 times.)

* IMG_7231 (2).JPG (726.87 KB, 1000x750 - viewed 362 times.)
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