Hi all,
I have a problem with jogging the motors in Mach 3. At this point the DRO moves and the config has been completed as per the Mach 3 tutorial.
The motors hold when powered from the Gecko 203V. i was on the phone with the BOB and we ran some checks and moved some jumpers etc to verify the BOB is working. He's confident that it's serviceable. He was of the opinion that Mach 3 might not be set up correctly.
At this time when measured at the BOB I have 4.8V between 2/com and 3/com. This doesn't move to zero when being jogged in Mach 3.
I removed the parallel cable from the PC and measured the voltages at the port. Between 2/25 up to 15/25 there is 5.0V present at all times.
Does anyone have any ideas about where to look?
Thanks
Ramon