I am using Pokeys (pulse engine) with mach3 062 version so its one before latest and the pokeys plugin is from May. Its used on a VMC retrofit with DC servo drives, my steps per mm are 393,7008 (2000 rev) on 5.08mm (0.2 inch) pitch ballscrew so one encoder count is 0.00254 mm.
Problem is , among other strange behaviors with homing which I will post in separate thread, that MPG works only with increments down to 0.02 , anything lower and it will not respond to MPG.
MPG is handled trough pulse engine and everything is setup as in manual. Looking at the settings page of Mach screenset MPG1 velocity and count are responding but I get movement only when the increment is set to 0.02 or higher.