I currently run this:
HiCON Plugin: 1.08.06, Target_Mach4_Build: 2491, Board: 7766, Serial: 8BBFDD, FW: 2.58, FPGA: 7E7B, IP: 192.168.0.35, AdapterIP: 192.168.0.10
Will try to upgrade to FW 2.59.
Do you think the crash issue is has anything to do with the Integra?
I still get the motion buffer out of sequence error when trying to jog. Any suggestions?
I use RL1 on J11 to ground a contactor (RLC = GND) wich controls my spindle motor. Cant get it to click.