Hi,
I'm currently trying to use a Linistepper V1 along side Mach3 to control 1 stepper motor. I have my step and dir signal going to the Linistepper driver and I am able to successfully and smoothly move/step the motor in one direction however when I try to move to the opposite direction(--) the motor gets loud and does move but very slowly.
What is odd is that if I switch the state of the "Step LowActiv" in the ports & pins / motor outputs tab I am able to move the motor in the direction that I previously couldnt, but once ive changed the step lowactiv state i am then unable to move in the other direction(++). This leads me to believe that Mach could be the issue.
Anyone bump into this before?