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Messages - khalid

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131
My This software is Free for everybody.. This software convert standart DST file format into Gcode.. The coding is little complicated but you will get 100,000 lines of Gcode within a second...

I am really thankful for Rene for working and thinking out of the box to get this software a new life..
The software also backplot each stitch movement and can give you time estimation of each thread color.. It also stop the machine in needle upward condition for thread change..

More can be seen
www.my-woodcarving.blogspot.com

132
Hi Rich,
I have checked the Gib Tighteness... Following were my observations:

1- The Y-axis Ball screw has 3inch dia pully installed.. I removed the belt and rotated the pully with One thumb and 3-Fingers... I was feeling the force of moving the Slide... The Screw has some spring action inside.. The wheel is turned first upto a limit with the screw and then screw nut takes the load and further after quarter turn the slide was moving...

I then adjusted the Taper wedge.. and now my Y-slide is moved with only two fingers and not enough force... For comparasion i would say i have reduced 50% force for movind the slide by loosening the taper wedge... I also checked the slope and it was un-noticable... The slide is very very Free now

2- The same procedure was adopted for my X_slide and it is also improved 50% from the previous...

Today i recalibrated X and Y axes as i have loosen the gibs.. I Did some real drilling on the SS-316 tube sheet of one of the exchanger we are fabricating... You can see the centre drills and two 8mm deep drills... The OTL (Outer Tube limit)is under 0.03mm... I also measure 14holes across and the commulative length is under 0.02mm...Now, I can drill SS-316 upto 33mm deep ...

The slides are very free moving after loosing the taper wedges..It seems that i have installed the linear rails
I am planning to make the new spindle with AISI 4140...Today I have hardened 03 different cylindrical pieces( dia: 1inch, length 1.5") of AISI 4140..
Each piece was heated to 850C and then one piece was Oil Quenched, One was Normal water Quench whereas the last one was quenched in the chilled water...
I have observed the longitudinal crack in the normal water quenched workpiece...

Following are the hardness results of 4140 test pieces..

A) Oil Quenched: 38.8HRC
B) Normal Water (Amb. temp): 54.1 HRC
C) Chilled Water: 49.8HRC

I cut half the option B, material and again taken the readings at the centre. I got 50HRC...That is excellent for spindle... For a good spindle the hardness must be in the range of 50~57HRC..

The Spindle is roughly machined out of AISI4140... I am going to Quench it on monday..

I am thankful to you for helping me...


133
Looks good, the backlash seems to be working ok on the Z otherwise you would have dug into the paper with the pen and tracking ok in the
x & y.
What F did you run it at?
Did you try cv and exact stop?

Actually i modified the PEN a little .. The pen comes with spring and on One click the point comes out and on the other click the tip get inside.. I modified it a little and it worked very fine as you have seen in the picture..

I ran the Gcode with F10 and i used CV mode On...
After running the program did you bring the Z down and see if it returned to the starting point? If it ran well at say one F, just double the feedrate and
 run it again since you returned  to the starting point, see if it tracks the same line and returns to the center starting point. At some F she will skip
and then you will know the max velocity you can run at. Then limit it to say 50 or 60 % of ( the 50 to 40 % reduction allows for torque required for cutting).
Yes the Program return to its exact start point..and the Z when commanded to go to zero, it exactly went to the zero location... I imported yours Gcode into NCPlot and exported in DXF... I open the DXF in AutoCAD and measured some dimensions and compared it with the pen-tracing... I was within 0.07mm range.. Amazing:)... As it was on the Paper so measurement was not easy by Vernier calipre;)

I just tried if with F10, tomorrow i will increase the velocity and will show you some more results:)... Lets say F10 is my maximum velocity then i have to keep my rapid F5 and keep the cutting 4IPM....Am I right.. My Stepper motors are for 80Volts rating with 4.2Amp per phase..Currently i am only supplying 36Volts DC.. I have connections of 48Volts and 60Volts too.. I will try increasing the voltage...

It is now clear that My Y-axis i.e. the bottom carriage , loosing steps.. This is because it carries the load of X-axis carriage+Workpiece load+Cutting forces.. It is boxway design so having frictional forces too (although i have appled Oil too)...






Then you can use a end mill to do some cutting in some scrap piece experimenting with some cut depths.

After playing around you will have some level of confidence on the F /  max velocity you should be using along with anticipated accuracy.
I will sure do so.. I am planning to use 1mm DOC for Aluminum... My Z-axis has some play, in the impeller case the Gcode was 2mm per pass and the first pass of the impeller was 3.5mm.. That was too much for the cutter..... so i will use shallow cut in future...

---------------------


Your original program had short straight line segments instead of the arcs.That can create a problem for YOU depending on the accel values
and mode you are running ( cv or exact stop ).

Yes, today i figured out how to output the gcode in G02/G03 IJK mode.. so in future i will make my Gcode more clean.. I am also planning to Use EXACT STOP MODE for milling... I hope that for better usage of Backlash compensation i should not use CONSTANT VELOCITY MODE...


Let me comment that in your program you clean out the bulk of the material in the first area and then finish the first vane of the impeller , then
 the others go on to profile the vanes only. Do as you wish, but, i would have cleared out all the bulk and then profiled the impellers.

Like said before, wood is different than cutting metal, so fool around to gain experince with YOUR machine.

"SPEED WILL COME UNBIDDEN ONCE ACCURACY IS ATTAINED"  ;)

RICH
The Gcode for the above impeller was made in ARTCAM.. and I know artcam is good for wax/wood but not for metal... I will use VisualMill for my next Gcode generation projects... I will follow your advice and will post you some good results..

Thanks for being with me and helping me:)

ONE QUESTION:
If my motors do not loose steps.. Then will the Backlash compensation will be OKAY for heavy Cuts?.. I read somewhere that Backlash compensation do not work for heavy cut.. Please enlighten me:)

134
Hi RICH... I modified my PEN and it is working right now:) Attached picture is the result of the Gcode you provided...

135
Hmm...Thanks RICH:).. I will definetly try it tomorrow and will show whats comeup with the setup:)

136
Hi RICH,Thanks for coming back and the file... I just watched your file and the code contains IJ parameters ..  so should have to change to IJ mode in Mach3.

I will defintly try it tomorrow and show you the results:)

137
Following is the Header of my impeller Gcode:
G90
G70
G40
g20
g64


I enabled the G64 (CV Mode is ON)...
Should this CV mode be on when we have backlash compensation ON?...

Regards

PS:
I used Quantum a lot in past without backlash compensation On and it gave me satisfactory results.. I am using QUANTUM MACH3 Version R2.43..
I have following settings to AntiJersk compensation as can be seen in Picture attached

138
General Mach Discussion / Re: Backlash compensation
« on: June 06, 2010, 10:01:47 AM »
Is it true.. Is it implemented in the latest version Mr.Barker?

139
Some More informations...
The machining/pocketing of part was carried out with TOOL rotating CCW and Table rotating CW as shown in Picture..
Flood coolant was ON with 3-High Pressure high flow jet Nozzles... for the above conditions :

I plunge the Tool using Ramping technique for the Aluminum Impeller..
Ramp ANgle= 10mm
Ramp Height= 12mm
Ramp distance= 10mm
The same ramp with 5IPM and the cutting speed was 8 IPM, using HSco 2Flute 8mm end Mill...


Again , i don't know why my Z-axis goes down in the work piece... In CAM i gave 2mm DOC/Pass for the above Aluminum part and the first Pass i measured was about 3.5mm.. there is some clearances in the Quill i think that once adjusted for the first pass and then for the next consequent passes it gives me exact DOC...


The backlash compensation was done in Mach3 and in the Circle and rotated square i am getting 0.01mm tolerances and no sign of backlash.. I afraid that this is done in no-l;oad condition... But if Mach3 compensate the backlash then the problem should not appear in actual work piece...
One other thing i want to share here, is that i installed the dial guage on the tooltip.. and gave lateral movement to the quill by hand i was getting 0.5mm flex... so total flex will be 1mm that will appear in workpiece..
This is the reason I am currently making drawings of a spindle... and will change the complete Z-axes...
Do i have to rework on my X/Y cross slides?.. These slides are boxway type and very rigid.. I feel no vibration in them.. Just to check the Tramming tomorrow...



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