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« on: January 12, 2013, 01:51:31 AM »
I'm STILL messing with my index pulse on this lathe conversion of mine. Per some recommendations off this board I converted the signal from the C3 into differential to the BoB due to some potential noise issues. I painted the index wheel flat black to avoid any optical errors. Mach is configured to allow syncing and has spindle speed averaging. The RPM readout seems to be very stable and doesn't hop around at all. I tried to thread for the first time tonight. The test piece was delrin and I was attempting to cut a RH 1x8 UNC thread 2" long. The first 3/4" or so of thread looks great, but then it looks like maybe one of the index pulses got dropped and the rest of the pitch is shifted over 1/2 of the thread pitch. It seems to correct at the beginning of each new cut since literally the first 3/4" or so looks perfect. It seems to be exactly half the pitch so a dropped index signal makes sense except for the fact that I've got averaging checked. It seems like the first few passes are great, but into the 3rd or 4th pass the thing starts buggering up. It has consistently done it 3 times now. I have noticed that I am getting a very consistent pulse out of the index LED on the C3 board and on the input in the BoB LED, but often times when I'm rotating by hand the LED on the diagnostic screen misses pulses here and there. I suspect there is something going on related to this but at this point I don't know where to look. I'm really desperate to get this machine threading due to a job I need to get out of here ASAP.
AAAAHHHHH!@#!@$!