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General Mach Discussion / Re: No communication between computer and controller box.
« on: December 21, 2016, 02:11:40 AM »
Looking at you .xml file…
The Step & Direction pin allocations in Motor Outputs do not match the .pdf document (manual) you have attached in post #22.
If you are using Estop then you need to allocate a Port# in Input Signals.
In Motor Tuning I suggest you change the Step Pulse and Dir. Pulse to 2uS.
Perhaps also try changing the Step Low Active State in Motor Outputs (from cross to tick) and see if that makes any difference.
Tweakie.
The Step & Direction pin allocations in Motor Outputs do not match the .pdf document (manual) you have attached in post #22.
If you are using Estop then you need to allocate a Port# in Input Signals.
In Motor Tuning I suggest you change the Step Pulse and Dir. Pulse to 2uS.
Perhaps also try changing the Step Low Active State in Motor Outputs (from cross to tick) and see if that makes any difference.
Tweakie.