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« on: May 31, 2018, 11:12:35 PM »
I was using the original Chinese control. It's hard to remember, but I know at one point, when running the demo it cut the material like it should. Something happened and would not plunge into the material and the pattern that it followed didn't appear to follow the roadrunner. I gave up and got a new enclosure with a Gecko G540, mean well 48v 12.5a PSU, rewired the steppers. After all that it's still not working. I can jog XYZ with my keyboard, but can't run a job. I'm baffled. I must be doing something wrong in Mach3. Just can't seem to figure it out. Motors are (X 23 green green 1 1) (Y 45 red green 1 1) (Z 67 red green 1 1). X had to be reversed. Inputs are just the Estop (enabled 1 15 red red). No outputs. Motor tuning was based on Axis calibration. X (400 2800.2 11.6675 3 2) Y (384 2800.2 17.132161 3 2) Z (182.8571429 2800.2 300 3 2). Don't know if I'm missing something. I'm wondering if I may have a defective UC100.