Machsupport Forum
Third party software and hardware support forums. => PoKeys => Topic started by: budgen30 on August 17, 2021, 10:06:48 AM
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Hello,
When i run a g-code program with G96 (Constant surface speed), my Z-axis jumps in feed speed randomly.
It wants to go full speed for a very short time. so the axis jumps a few cm during the program.
There is no error and when i run the same program again, the moment is different each time.
the code is just normal.
I found out when i run normal (without CSS) or jogging or a MDI G1 code there is no problem.
My RPM readout is stable.
I have the latest version of mach4 hobby (licensed) and pokeys57cnc
what can be the problem?
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I narrowed the problem to: feed per revolution.
if i do feed per revolution (FPR) in my g-code i have this jumping feed problem.
if i do CCS + normal feedrate mode the jumping is not there.
if i do CCS + FPR there is jumping
if i only do FPR (without CSS) there is also jumping
maybe the RPM readout is not steady enough for FPR?
i use 1 signal per revolution. i have tried my rpm high speed filter at 100 and 500. makes no difference.
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hello,
I have a quick update. I read a post about electrical noise.
I notices a mini fraction of a second that the rpm was out of control (and the reaction of the machine jumping)
first i upgraded my aluminium sensor wheel with a magnet for a stronger detection signal. (aluminium gives a weaker signal).
The was better but the problem was not completely gone.
I checked my cable of my rpm sensor. i had bound the cable of the sensor to all the other wires of my machine. I isolated it from them: separate routing of the cable and i gave the cable a metal cover (metal speaker cable sleeve) from start tot the pokey board connectors. I also put a thick metal plate between my servodriver and the pokeys57cnc.
After these mods the problem was gone!
I hope it will stay that way.
I tried the same programs and threading, which went ok.
Regards!