Machsupport Forum
G-Code, CAD, and CAM => G-Code, CAD, and CAM discussions => Topic started by: CNC_Guitar on January 28, 2015, 05:55:29 AM
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Hi All,
I used the demo file "scorpion.tap" to test my router table.
This file is part of the Mach3 demo version.
When the g-code is processed and the mill has to go back to it's zero point , it happens that the Y-axis motors (slaved-axis) seem to jam (it does'nt sound good :'().
The result is that the Y-axis does not go back to zero and I need to home the table again.
I'm quite sure that the settings in Mach3 are ok and both motors (y- and slave axis) are tuned exactly the same.
Jogging (fast/slow) and homing works ok.
Does somebody have an idea what could cause this problem?
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Hi would appreciate if you have manage to solve your problem. I have been looking into changing my Chinese board problem and fitting a smooth stepper USB or Ethernet? How easy or tough is this to do , any wiring diagram set up would be much appreciated.