Hi Tom,
The problem is still unsolved.
I've used the following G-code.
G90
G0 X0 Y0 B0
M7
M9
G1
X 26.0 Y 0 B 19.5 F 300
X 27.0 Y 0 B 39.0 F 300
X 28.0 Y 0 B 58.5 F 300
X 29.0 Y 0 B 78.0 F 300
X 30.0 Y 0 B 97.5 F 300
And the macropump.m1s was:
SetModOutput(81, GetOemDro(804))
B-axis setting was in a way that B1 command output the analog output value 1.
In theory, B4095 should output 10V. And when we checked B command on DMI, it worked.
The problem is that when we run the G-code above, as soon as B command starts being used, the motion stops.
Interestingly, the G-code still runs without any machine movement.
Do you know what the problem is?
Best Regards,
Eric.